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Member Since: March 2, 2010

Country: United States

  • Thanks for the response!
    I will contact tech support.

  • ang.mack
    I am having the exact same problem with this IMU. The accelerometer outputs are rock solid, but the gyro outputs take quite some time to return to zero after movement stops. In Fact, the gyro output seems to over shoot zero and since I’m integrating the data and accumulateing it in a single variable, the initial move is canceled out.
    I would appreciate any guidance anyone has to offer.

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